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Improving on a Good Thing:
Romo Reduces TRI Releases
Romo Incorporated, a screen and digital printer in De Pere,
Wisconsin has been nationally recognized (see references below) for its
leadership efforts in adopting and sharing environmentally preferable materials
and work practices in screen printing. A strong focus on environmental
stewardship has led Romo’s management to direct a series of progressive waste
reduction efforts. This case study provides an update on Romo’s most recent
progress in its quest for continuous environmental improvement. Romo’s efforts
show how continued and focused commitment to waste reduction is needed to
sustain and build upon early successes, thereby providing maximum cost savings
and emission reductions.
Like many screen printers, Romo has a diverse repertoire of
products, from small decals for original equipment manufacture, through
point-of-purchase displays, to fleet graphics. The production equipment fits
into a 41,000 square foot plant built in 1992 and has allowed Romo to transact
over $9 million in sales for 1998.
Since its founding in 1953, the company has seen a tightening
of environmental regulations. In 1986, Romo made a corporate commitment to stay
ahead of the regulatory progression through pollution prevention. Romo’s focus
on source reduction of emissions enabled the comany to meet regulatory
requirements, avoiding the negative risks associated with non-compliance such as
potential high fines. More importantly, it put Romo in the proactive driver’s
seat of change, charting its own course with adequate investigation,
preparation, and travel time. Romo chose to focus on pollution prevention
because the company believes that it best enables the company to fulfill its
responsibility to provide both its employees and its community with a safe
environment.
The Search Begins
Romo decided to focus its initial efforts on the screen
washout area, a primary source of air emissions and hazardous wastes for most
screen printers. Screen wash solvent was being sprayed on dirty screens,
collected in an open tank, filtered, and reapplied. This process was using 20 to
40 gallons of virgin solvent per day. The filtering method did not sufficiently
remove the suspended solids from the solvents. Selected improvements included
covering the tank and adding a distillation system. For a cost of $2,900, these
improvements cut solvent use more than 90%. Further reductions were made when
the solvent delivery hose was equipped with an adjustable spray nozzle, similar
to those used on garden hoses. Brushing the screen with solvent before the wash,
and limiting the flow from the nozzle with a block of wood under the handle to
prevent its full travel, further reduced the amount of screen wash used on each
screen.
These two process changes reduced Romo’s toluene and methyl
isobutyl ketone (MIBK) emissions by 39%, from 30,400 to 18,480 lbs, between 1988
and 1991.
Next Steps
Having experienced the success of its initial efforts, in
1992 Romo joined the EPA’s 33/50 program. In doing so, the company voluntarily
set goals of reducing emissions from their 1991 levels by 33% in one year and by
50% at the end of the fourth year, 1995. A three-pronged approach was planned to
meet these goals, including:
- reduce the volume of all chemicals used;
- seek alternative application techniques; and
- improve selection of materials used.
Employee input was solicited from all levels and feasible
projects were chosen for each area of the production process. To qualify for
adoption, any change had to reduce chemical exposure risks to employees, reduce
pollution, and to be compatible with the other tasks in the production process.
After review of suggested improvements, Romo decided to focus
on improving the emulsion removal task and changing the press wash. Emulsion
removal was by the installation of a high-pressure washer. The washer improved
cleaning effectiveness while reducing usage of water and emulsion remover. In
fact, the emulsion remover concentration was halved while still producing the
same cleaning effect. Work processes were also modified to improve an initial
application of full-strength emulsion remover. Previously, this had been applied
by manual brush and resulted in excess application that dripped onto the
cleaning room floor. The new process uses a controlled spray, which uniformly
applies a thinner coat of emulsion remover, reducing dripping and waste.
Together, these improvements reduced emulsion remover purchases by 75%.
A new press wash recommended by other screen printers was
chosen. It cleaned with propylene glycol monomethyl ether, propylene glycol
monomethyl ether acetate, and cyclohexanone rather than toluene or MIBK. At the
end of 1992, less than one year into the 33/50 program, the toluene and MIBK
releases had been reduced by more than 70% to a combined 5,390 lbs. Romo had
surpassed not only the first year’s goal, but made such great strides that the
four-year goal was eclipsed. More details of Romo’s participation in the 33/50
program are available in the DfE screen printing case study: Reducing the Use
of Reclamation Chemicals in Screen Printing.
Further Improvements
Buoyed by their success in the 33/50 program, Romo swam into
the deeper waters of pollution prevention in 1996. Because of their commitment
to continuous environmental improvement, Romo’s managers decided upon a
proactive goal, to eliminate the use of all chemicals listed in the USEPA’s
Toxics Release Inventory (TRI). In order to implement the goal, they looked for
further emission reductions with new screen cleaning products. A "Solvent
Team" was formed consisting of employees who use the screen cleaning
solvents. Romo’s solvent vendor was able to supply some alternative products
and different samples were provided by other suppliers. Alternative products
were tested under production conditions. Data were gathered to document the
amounts used, any recommended changes in production procedures, and how easy the
products were to use.
After several months of testing, Romo’s Solvent Team chose
to adopt new products for its press wash, screen wash, and emulsion remover. The
active ingredient in the press wash is isobutyl isobuterate, and the screen wash
relies on propylene glycol ethers and other nonhazardous proprietary chemicals.
The chosen replacements do not contain toluene, MIBK, or any other TRI-listed
chemicals.
Impacts
Savings
Table 1 shows the change in chemical use before and after the
1996 switch. Unit costs of the replacement press and screen washes, designated
in Table 1 as ‘post-96', are higher than their ‘pre-96' counterparts.
However, the volumes used are substantially reduced, resulting in a net savings
of $3,170 per year, a reduction of 12.6%.
Approximately one quarter of the 1995 press wash use has
continued in 1998. The post-96 press wash has not been able to clean some of the
difficult jobs as well as the pre-96 press wash, especially when printing
halftone images. Hazardous waste disposal and labor costs did not change
significantly.
Table 1. Effects of 1996 Changes on Solvent Use and Costs
|
|
Amount Used
(gal/yr) |
Unit Cost
($/gal) |
Total Yearly
Material Cost |
|
Materials and Costs before 1996 Improvements |
Pre-96 Press Wash
|
2530 |
$3.26 |
$8,248 |
|
|
Pre-96 Screen Wash
|
1265 |
$13.30 |
$16,825 |
|
1995 total |
|
$25,072 |
|
Materials and Costs after 1996 Improvements |
Post-96 Press Wash
|
1045 |
$13.30 |
$13,899 |
|
|
Post-96 Screen Wash
|
385 |
$15.20 |
$5,852 |
|
Pre-96 Press Wash
|
660 |
$3.26 |
$2,152 |
|
1998 total |
|
$21,902 |
|
Annual Savings |
$3,170 |
A new emulsion remover is an integral part of the screen
cleaning process. The combination of new press and screen washes and emulsion
remover cleans so much better than the previous chemicals that the need for an
optional final step in screen cleaning, secondary haze removal, has been
reduced. Only 5% of the screens used in 1997 required haze removal, down from
33% of all screens in 1988. Two areas of savings result from this change. First,
fewer gallons of haze removing chemicals are purchased. Second, since the
screens’ exposure to the caustic haze remover is reduced, the screens are
replaced less frequently. Spent haze remover is captured in a drain trap which
requires infrequent cleaning and disposal, the costs of which are minimal and
have not changed appreciably.
Emission Reduction
Impressive waste reduction has been attained by Romo in this
round of changes. Table 2 depicts a total reduction in TRI chemical emissions of
64% between 1995 and 1998. Some rebound in emissions has occurred between 1996
and 1998. A portion of this can be explained by Romo’s fast growth, especially
in areas which require use of the pre-96 cleaning system.
Table 2. TRI Releases at Romo
|
|
Toluene (lb) |
MIBK (lb) |
Total TRI Releases
(lb) |
Change in Total TRI Releases (%) |
Change in Company Sales Revenue
(%, unadjusted for inflation) |
|
1995 |
9,106 |
3,984 |
13,090 |
|
|
1996 |
2,101 |
919 |
3,020 |
|
1998 |
3,749 |
937 |
4,686 |
|
Change
1998-1995 |
-5,357 |
-3,047 |
-8,404 |
-64% |
70% |
Future Plans
Romo plans to continue its progress toward increased
environmental stewardship with more basic changes in its printing materials.
Currently the only product used that releases a TRI-listed chemical is the
pre-96 press wash. This solvent is only used to clean solvent-based inks. As
part of its ‘zero TRI reportable’ goal, Romo has been working to reduce its
use of solvent-based inks, replacing them with UV-cured inks. In the midst of
the changes described here, UV ink use continued to increase from 40% of Romo’s
total ink volume in 1995 to 60% in 1998. Individual product lines are converted
to UV ink through the expertise of Romo’s research and development team. More
progress is planned for the future. Based upon their success with UV inks, Romo
is committed to completely phase out solvent-based inks, expecting to reach its
goal of eliminating all TRI releases by 2003.
References
Details of Romo’s participation in the 33/50 program are available in the
DfE screen printing case study: Reducing the Use of Reclamation Chemicals
in Screen Printing, EPA 744-F-93-015, available from the Pollution
Prevention Information Clearinghouse, 202-260-1023, or www.epa.gov/opptintr/dfe/screenprinting/case_studies/case1/!project.pdf
Romo was awarded an 1997 Environmental Champion award by USEPA and Chemical
Engineering Magazine. A description can be found at www.che.com
A video case study describing Romo’s recent pollution prevention
activities is contained in Using Screen Printing Technologies for Business
and Environmental Success. A videotape with written description is
available from PNEAC.
Romo’s Quality Manager, Jon Weber, can be reached at 920-336-5100, jweber@romoinc.com.
The Screenprinting and Graphic Imaging Association offers technical
assistance to screenprinters. Visit SGIA’s web site at www.sgia.org
or contact Marci Kinter at 703-385-1335 or marcik@sgia.org.
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