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United States Environmental Protection Agency
Air and Radiation
EPA 600-SR-93-149
REPLACEMENT OF HAZARDOUS MATERIAL IN WIDE WEB FLEXOGRAPHIC
PRINTING PROCESS
The Lustreprint Company hosted the test and operated the
equipment. Test design and management was by Erie County Environmental
Compliance Services, (ECECS), Buffalo, New York. The test personnel were
supplied by Recra Environmental, Incorporated on contract to ECECS.
Technology/Testing
A wide web flexographic printing firm substituted water-based
inks for solvent-based inks when manufacturing flexible packaging, using plastic
sheet substrates (e.g., plastic bags for bread). The project objectives were to
evaluate the technical feasibility (particularly as related to process
implementation and performance), the economic effect, and the resulting change
in VOC emissions achieved by the substitution. The technical evaluation was to
quantify the reduction in both volatile and liquid-phase solid hazardous wastes.
This is a study of the effectiveness and applicability of ink
substitutions to reduce waste in a wide web (greater than 16 in. wide)
flexographic printing process. The Lustreprint Company prints flexible packaging
whose products are used in the food and snack industry and in medical,
industrial and consumer applications. Printing is completed on a number of
different web materials, (commonly polypropylene (acrylic coated, Saran coated,
and uncoated corona pretreated), cellophane (Saran coated), polyester (both
metallized and unmetallized), polyethylene. and nylon (both Saran coated and
uncoated)). At the time of this study, Lustreprint used one Hudson/Sharp 48 in.,
central impression six-color flexo press and one Heinrich (W&H) five-color
flexo stack press.
New York's regulations require that a facility reduce overall
plant emissions to within the compliance level of 100 tons/yr. As an option,
Lustreprint chose to reduce the use of solvent-based inks and adhesives. The
first step eliminated solvent-based adhesive used in laminating. This was
followed by a phase-in of water-based inks in the printing operation. The
company goals are to reduce all volatile organic air emissions to an extent that
would eliminate the need for costly air abatement and permitting and to
eliminate all liquid-phase solid waste, at the facility.
To achieve these goals, ink use was monitored over four, one
week long, study periods: 3 weeks when both water-based and solvent-based inks
were used and 1 week when only solvent-based inks were used. Historical data for
emissions and waste generation were extrapolated for comparison with the weekly
experimental data. From the 4-week ink use and waste analysis data, the VOCs,
released as emissions from the printing process, could be calculated. A material
accounting approach was used for three calculations. All liquid wastes generated
during the test periods were segregated and analyzed for percent volatile
constituents. Substituting water-based inks required press modifications.
The most significant retrofit was installation of an Enercon
corona discharge treater.
Modifications to the Hudson/Sharp 48 inch, central
impression, six-color, flexographic printing press included upgrading drying
capacities and using enlarged exhaust and supply fans.
Because of prohibitive costs, the Heinrich (W&H) press
was not modified or retrofitted and was not used in the water-based ink tests.
Future plans would include replacing this press with one that could accommodate
the ancillary equipment required for water-based ink use.
Ink metering rolls were replaced to facilitate drying. Pumps
were also replaced to accommodate the new printing inks. Additional ductwork and
noise abatement equipment were needed.
Table 1 shows the VOC emissions as a function of ink use,
based on historical data.
TABLE 1 VOC EMISSIONS BASED ON INK USE 1990
|
Month |
Ink used
(lb/wk) |
VOCs calculated
(lb/wk) |
|
April |
3,038 |
2,111 |
|
May |
1,681 |
1,700* |
|
June |
2,686 |
2,289 |
|
July |
2,109 |
1,731 |
|
August |
2,945 |
2,345 |
*This value is derived from the historical operational data and attributed to
high makeup solvent use during the event.
Table 2 provides information on the total pounds and percent
of ink used, calculated VOC emissions, and VOC emissions as a percentage of ink
used for each of the four 1-week-long evaluation periods.
A review of the quality assurance sheets indicates that the
use of water-based inks typically did not change product quality although some
problems arose after customer use, depending upon the ultimate use of the
packaging, what the package contained, and the means by which the packages were
sealed. Heat and stress of the printed package material caused by the package
folding and sealing process at times resulted in a loss of ink adhesion.
Some combinations of water ink and solvent ink were
incompatible. Water inks did not provide a consistent opaque white for
lamination to cover metallized films and resulted in "blocking" (or
transfer of print) when printing on Saran-coated materials, especially
cellophane. In most cases, however, depending on the surface printed, no
difference was noted with the use of water-based inks.
Normal propyl alcohol added in small amounts (less than 1%)
to prevent water ink foaming at the ink pan and to assist in ink wetting was
beneficial. Variations of the pressure sensitive "stickyback" material
used to attach the printing plates to the plate cylinder (solid versus cushioned
stickyback) also enhanced printed solid plate backgrounds without pin-holding.
The plate material may also have an effect. Photo polymer plates work well with
water but are more expensive than rubber. Nylon plates are a possible compromise
with a longer life than rubber plates.
Table 2. Ink and VOC Emission Data for 4-Week Study Period
|
Measured Parameter |
Week 1 |
Week 2 |
Week 3 |
Week 4 |
|
No. of inks |
23 |
32 |
33 |
22 |
|
Solvent ink (lb) |
1,112 |
1,746 |
2252 |
549 |
|
Water ink (lb) |
1,251 |
508 |
0 |
688 |
|
Total ink (lb) |
2,363 |
2,254 |
2,252 |
1237 |
|
Solvent ink (%) |
47.1 |
77.5 |
100 |
44.4 |
|
Water ink (%) |
52.9 |
22.5 |
0 |
55.6 |
|
VOC emissions (lb)
(calculated) |
827.5 |
1,251.7 |
1,571.5 |
509.0 |
|
VOC emissions (%)
(% of ink total) |
35.0 |
55.5 |
69.8 |
41.1 |
|
Waste (lb) |
55.6 |
20.0 |
0 |
0 |
|
Waste VOC content
lb |
54.3 |
4.7 |
0 |
0 |
VOC Reduction
Substituting with water-based ink reduced the emissions
generated from the printing p each percent increase in water-based ink use, the
calculated reduction in VOC emissions was (Table 3).
As can be seen from Table 3, for Weeks 1 and 2, the VOC
generation decreased in proportion to the percentage of water-based ink used. A
52.9% water-based ink use resulted in a 53.3% reduction in VOC emissions.
Similarly, in Week 2, a water-ink use rate of 22.556 resulted in a VOC emission
reduction of 23.4%.
For Week 4, the corresponding reduction in VOC emissions was
less significant: a 55.6% water ink use rate reduced VOC emissions only 43.3%
Total ink use for Week 4 was 1,237 lb of combined water ink and solvent ink.
This amount is approximately half of the amount used during the other 3 weeks of
the study. The number of different inks used in Week 4 is, however, comparable
with that used Week 1. With the same number of ink changes at the printing
stations and with each change requiring a cleaning before adding new ink, the
amount of cleaning make-up solvent relative to total ink use is expected to
increase. The contribution of VOC emissions from clean-up solvents reduced the
effectiveness of VOC reduction by water inks.
TABLE 3, VOC REDUCTION
|
Week |
Total ink
(lb) |
Factored*
VOC (lb) |
Water ink
(%) |
Reduced
VOC (lb) |
Reduction
(%) |
|
1 |
2,363 |
1,772 |
52.9 |
827.5 |
53.3 |
|
2 |
2,254 |
1,634 |
22.5 |
1,252.7 |
23.4 |
|
3 |
2,252 |
1,633 |
0.0 |
1,571.5 |
0.0 |
|
4 |
1,237 |
897 |
55.6 |
509.09 |
43.3 |
*Calculated by taking 72.5X of the total ink quantity.
Waste Reduction
Historically, 315 gal of solid waste was generated each
month. This translates to approximately one-and-one-half, 55 gal drum or 424
lb/wk. The printing operations during Week 1 were an 87% decrease from normal in
solid waste generation (from 424 lb to 55.5 lbs); and 100% elimination of solid
waste generation in Weeks 3 and 4.
Note that much of this waste decrease can be attributed to
factors other than the type of ink used. The WRITE Program evaluation and the
use of the waste generation from increased awareness of press operators and
deterred waste generation. This induced press operators to reuse solvent for
additional cleaning or reuse in the solvent inks.
Economic Analysis
An economic analysis of the changeover from solvent to
water-based ink is included as part of this project.
Fixed, variable, and overhead costs are affected by this
substitution and are considered. Fixed costs include the purchase and
installation of new equipment (primarily the Enercon corona discharge treater)
and costs for replacing equipment ancillary to the central impression cylinder
press, such as pumps, dryer upgrade, ink pans, etc.
Variable cost adjustments include the premium paid, or
reduced cost, for water-based inks. Disposal costs were calculated by using the
amount of waste solvent ink generated in gals and the most recent disposal cost
figures provided by Lustreprint. Other variable costs included variations in
labor hours and utilities.
Overhead costs also play a role in determining the cost
savings. Items such as the time previously expended for regulatory compliance,
insurance costs, employee equipment and safety training, and OSHA compliance
were expected to be reduced as a result of removing hazardous waste from the
shop floor. These potential cost savings were estimated from existing figures
where available.
Based on these costs, payback period was calculated (Table
4).
The payback period could be further reduced by eliminating
the solid waste disposal. With the complete changeover to water inks and the
planned purchase of an ink splitter, at approximately $8,000, an additional
savings for solid waste disposal would be possible. The payback period would
then be reduced by 0.53 year.
TABLE 4. PAYBACK PERIOD
|
Variable |
Initial Investment |
Projected Savings |
Payback Period, year |
|
Current process revisions |
$62,901 |
$24,587 |
2.56 |
|
Adding an $8000 ink splitter |
$70,901 |
$34,887 |
2.03 |
|
Full water-based ink conversion |
$62,901 |
$117,078 |
0.54 |
Conclusions
By installing an in-line corona treater, higher surface
tension water-based inks could be used. This, in turn, reduced VOC emissions
approximately 72,5%, when compared with those for solvent-based inks. The
water-based ink formulas contain about 20% solvent. For a process using a
quantity of approximately 2250 lb of solvent-based ink (weekly), VOC emission
levels were about 1570 lb. For every 1% increase in water-based ink use, VOC
emissions were reduced 14 lb.
The substitution of water based inks did not adversely affect
product quality or nonhazardous scrap waste generation. Some changes in
operating procedures were, however, necessary because of the nature of
water-based inks. The average reduction of 95% of liquid F003 waste from waste
ink and cleaning solvents recorded during the study period resulted from
operational practice changes.
The payback period for the corona treater and equipment
modifications is 2.56 years. Additionally, through segregation of wastes once
full implementation of water-based inks is achieved, the payback period could be
reduced to 0.54 years.
This successful implementation of water-based inks in
flexographic wide web printing should be considered as a VOC source reduction
method for similar printing operations.
Report
The full report, entitled "Replacement of Hazardous
Material in Wide Web Flexographic Printing Process" by P.B. Kranz, et al.,
is available as EPA/600/SR-93/149.
For more detailed information about pollution prevention opportunities in the
printing industry visit the PNEAC web site at www.pneac.org
, call the PNEAC toll free number at 1-888-USPNEAC, or contact :
- Graphic Arts Technical Foundation - Gary Jones or Rick Hartwig
(412/741-6860)
- Printing Industries of America - Ben Cooper (703/519-8115)
- Illinois Hazardous Waste Research & Information Center - Gary
Miller (217/333-8940) or Debra Jacobson (630/472-5019)
- University of Wisconsin - Wayne Pferdehirt (608/265-2361), Keith West
(920/465-2940) or Bob Gifford (608/262-1083)
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